So,
Managed to start her up for like 3 heat cycles. I made some minor modifications. There was a gearbox oil leak so got it fixed. I putted a 162 main jet in the carb, needle on the 2nd from the pointy end. It was awesome. Waay waay better than it was, I was really suprised. Its too lean now too!
Altough I am happy, Im kinda sad too. After the 3. Heat cycle I saw little bubbles in the water pipes. That means the head O-ring blew up. I was right.

Will fix it on the next week. Will machine a bit angle in the cylinder head, where the O ring meets with it. It will give a better seal, thats for sure. Will put a thicker O ring in there too.
First is how it will look like and the second is what it is now.
